The port operator had not implemented an effective planned inspection and maintenance program for the mooring system in Flying Fish Cove. Consequently, it had been 18 months since the underwater components of the cantilever line had been inspected.
Bowen Tug and Barge had identified the need to spread the slings when lifting a stores container. However, there was no process in place to ensure that ships' crews were advised of this to ensure its safe return from the ship.
Bowen Tug and Barge’s safety management system guidance for barge storing operations did not designate roles or responsibilities to specific individuals and a system for communicating with the ship’s crew was not discussed and established.
Compliance auditing on board British Beech had not identified that requirements of the job hazard analysis were not being followed by the crew during the storing operations.
The lack of any record of incident reporting by Bowen Tug and Barge, and its employees, indicates an ineffective reporting culture within the company. Hence, the opportunity to learn from previous incidents was lost.
Bowen Tug and Barge did not have an effective compliance auditing process in place to ensure that its employees were following the training they had received and the guidance contained in the safety management system documentation.
Adonis’s safety management system did not contain any procedure or guidance in regard to the use and correct setting of the tug’s towing hook quick release arrangements.
The location of the towing hook ‘locking’ pin on the upper part of the quick release lever meant that if the pin was not properly in its ‘unlocked’ slot, it could fall into the locking hole, thereby locking the release lever.
The requirement in Sea Swift’s Marine Execution Plan to let Adonis go after clearing the Clinton coal wharves was ambiguous and this led to the crews of Adonis and Wolli misinterpreting the requirement.
MSC Siena’s permit to work over the side and the associated procedure required that the ship not be underway when working over the side. However, this requirement could not be complied with when working over the side to rig a combination pilot ladder.
MSC Siena’s safety management system procedure for working over the side required that a risk assessment be carried out, and necessary checks and precautions documented in a work permit. However, the procedure had not been effectively implemented on board the ship.
Brisbane port authorities had not put in place sufficient procedures, checklists and/or supporting documents to ensure VTS staff were adequately prepared, trained and practiced to handle a predictable incident such as this.
The design of the burner nozzle allowed the nozzle swirl plate and needle valve to be misaligned when being assembled which in turn led to the needle valve stem being damaged during assembly. Furthermore, the maintenance manuals and supporting documentation supplied by Garioni Naval, the thermal oil heater manufacturer, did not provide sufficient guidance to ensure safe and appropriate maintenance of the thermal oil heater burner assembly.
While the Flinders Ports passage plan for Port Lincoln contained information relating to general navigation in the port, such as depths and navigation/channel marks, it did not contain actual passage specific information, such as courses and speeds to be followed. If the plan had contained course and speed information, the ship’s crew would have been better prepared for the pilotage.
Flinders Ports had not undertaken a risk assessment, or developed contingency plans for this specific shiphandling manoeuvre in Port Lincoln. Consequently, the pilot had no guidance regarding what actions to take if the berthing manoeuvre did not progress as he planned.
When the main engine was operated in engine room control mode, there was no automatic interlock to prevent ‘wrong way’ operation of the engine and no audible alarm to indicate when it was running the ‘wrong way’. As a result, the only system protections to warn the crew of ‘wrong way’ running of the engine were the bridge and engine control room console mounted flashing light indicators.
The participation of the two tug masters in the pilotage process was not actively encouraged in Port Lincoln. Consequently, it was not until after the collision that one of the tug masters advised the pilot that the ship's main engine was still running ahead.
Newlead Bulkers had not implemented any procedures or guidance to inform the crew that extra vigilance was required when operating the main engine in engine room control mode because there was no automatic interlock to prevent ‘wrong way’ operation of the engine and no audible alarm to indicate when it was running the ‘wrong way’.
The shipyard commissioning processes did not identify that the ship’s rudder angle indicator transmitter and tiller link-arm were not installed correctly.