The ATSB has found that an undetected flaw, and the subsequent failure of a critical main engine component, led to the bulk carrier Enterprise being disabled in Bass Strait on 10 July 2006 and drifting for nearly three days.
The Australian Transport Safety Bureau investigation has found that a microscopic flaw led to the failure of a main engine gudgeon pin. The investigation also found that the engine manufacturer did not provide sufficient guidance for monitoring the fatigue life of gudgeon pins and that the planning and execution of maintenance on critical items of equipment was inadequate…