Output Number
Approval Date
Published Date Time
Recommendation type
Mode
Date released

The Bureau of Air Safety Investigation recommends that the
engine manufacturer AlliedSignal audit the process employed to
manufacture TPE 331 turbine wheel knife-edged seals, to determine
those factors that may lead to excessive variations in slot corner
radii.





As a result of the investigation into this occurrence, the Bureau
simultaneously issues the following interim recommendations and
safety advisory notice:





IR19990113



The Bureau of Air Safety Investigation recommends that the engine
manufacturer AlliedSignal determine the sensitivity of turbine
wheel seals to the initiation of fatigue cracks from slot corners,
as a function of slot corner radii.





IR19990114



The Bureau of Air Safety Investigation recommends that the engine
manufacturer AlliedSignal consider, during engine design and the
formulation of continuing airworthiness instructions, the
possibility that turbine wheel seal fatigue failure may result in
hazardous modes of engine failure.





IR19990115



The Bureau of Air Safety Investigation recommends that the Civil
Aviation Safety Authority Australia conduct an audit of that part
of the aviation safety system that establishes the operational
history of life-limited components, to establish why the
operational history of second-stage turbine wheel, p/n 868272-1,
s/n P03214C, could not be determined with certainty.





SAN19990116



The Federal Aviation Administration should note the safety
deficiency identified in this document and take appropriate action
as considered necessary.

Organisation Response
Date Received
Organisation
Allied Signal Aerospace
Response Text

Please find attached AlliedSignal's planned actions and
AlliedSignal's Materials Analysis (MA) of the 2nd stage turbine
wheel from the subject incident.



Based on the MA and review of the engine hardware, AlliedSignal
believes that an improper repair of the 2nd stage stator assembly
resulted in blocked cooling passages which resulted in reduce
cooling flows and higher operating temperatures in the inner
support region. This resulted in the separation / uncoupling of the
curvic seal from the 2nd stage wheel followed by the uncontained
separation of the 2nd stage turbine wheel.



Upon completion of the planned actions associated with the interim
recommendations, I will forward any results and/or process
changes.



If you have any comments or questions, feel free to contact me via
E-mail Thank you for the opportunity to respond to these
recommendations.





IR19990112



AlliedSignal agrees to audit the manufacture of TPE331 turbine
wheel knife-edged seals by March, 2000. The audit will focus on the
manufacture and inspection of the slot corner radii, including the
applicable paperwork. However, it has not been our experience that
these slot corner radii have exhibited excessive variation with
respect to design intent.



Furthermore, AlliedSignal does not believe that the seal corner
radius was the primary cause of the wheel separation of engine
P-03214C. Material analysis performed at AlliedSignal indicated
that the primary contributing cause was the cooling flow blockage
resulting from improper repair of the second-stage stator assembly.
This blockage resulted in higher than normal operating temperatures
for the knife-edged seal, which we believe led to the uncoupling of
the seal from the wheel and subsequent damage. This small fatigue
crack observed was believed to be secondary to the uncoupling of
the seal from the wheel. Additionally, this knife-edged seal design
has accumulated over 30 million operating hours without any
instances of fatigue separations.