On 22 August 2003, a Reims F406 aircraft, registered ZK-VAF, was
being operated on a passenger charter flight from Darwin to Tindal,
NT. At approximately 85-90 kts during the take-off roll, the nose
landing gear (NLG) collapsed. The aircraft slid to a stop, the
pilot shutdown the engines and all occupants evacuated the aircraft
uninjured. Prior to this occurrence, on 2 and 19 June 2003, pilots
reported difficulties obtaining a `down and locked' indication for
the NLG. Maintenance actions rectified the problems at that
time.
An examination of the aircraft following the NLG collapse
revealed that no damage was evident to any NLG components, or the
NLG attachment structure. The NLG rigging was checked and reported
to be within tolerances. Damage to the aircraft included abrasion
damage to the lower forward fuselage and NLG doors. Both propellers
were substantially damaged from ground contact.
The NLG hydraulic actuator was removed from the aircraft for
further examination by the ATSB and was taken to a specialist
hydraulic facility for functional testing prior to disassembly. The
actuator passed all required functional tests, however, it was
noted that the integral microswitch had been incorrectly adjusted
to the point that it did not obtain switchover during operation of
the hydraulic actuator. The microswitch was effectively always
providing a signal indicating that the actuator was `down and
locked'. However, as the actuator microswitch was wired in series
with the NLG overcentre microswitch on the aircraft, the landing
gear indications would have appeared normal. The aircraft landing
gear hydraulic system was powered during landing gear extension,
however hydraulic power was removed once all three landing gear
downlock microswitches were activated.
Disassembly of the NLG actuator revealed that all internal
components were in good condition, with only minor wear evident.
The actuator rod-end was noted to have an incorrect locking washer
fitted. A detailed examination of the actuator components revealed
that the installed locking washer did not conform to the part no.
NAS 559-1 locking device specified by the actuator Original
Equipment Manufacturer (OEM). Refer to Appendix A, Figure 1.
Comparison against Original Equipment Manufacturer
component
An OEM locking device was obtained and compared against the
installed washer. The OEM item was a key-like component and
utilised a completely different mechanism for securing the assembly
from the installed washer. The installed washer was placed between
the rod-end and the lock nut and had a small tang that fitted into
the rod-end shank keyway, but was not lockwired. The OEM item
fitted into the keyway completely, lying underneath the lock nut
and engaged with the slotted end of the actuator rod when the lock
nut was tightened. The OEM item also provided for the installation
of a locking wire between the drilled rod-end lock nut and the
locking tab. Refer to Appendix A, Figure 2.
Damage to the installed washer
The washer that was installed to the rod-end assembly showed
clear evidence of rotation against the underside of the lock nut
and the actuator rod-end face. Two sides of the washer had been
bent in opposing directions, against the respective flats of the
nut and rod-end. The bent areas showed damage consistent with
repeated manipulation and re-bending of the `tabs'. The small
locking tang on the internal diameter of the washer had fractured,
allowing the washer to freely rotate on the threaded rod-end shank.
The fractured key tang was recovered from the rod-end keyway and
cleaned to allow stereomicroscopic examination, which showed that
the tang had broken away from the washer under sideways bending
overload, such as would be produced by forces acting to twist the
washer around the rod-end shank.