A Boeing 717 aircraft was in a left turn holding pattern,
descending through flight level 230, when the right engine shut
down. The flight crew actioned the emergency procedures and
attempted, unsuccessfully, to restart the engine. They notified air
traffic control of the problem, then requested and received a
vectored straight-in approach and landing.
Following the event, the operator's maintenance personnel
conducted troubleshooting of the right engine. Several fault codes
were noted in the computer memory, which related to Channel A of
the electronic engine controller (EEC). A maintenance records check
found that the right engine fuel metering unit (FMU) had been
replaced approximately 50 flight hours prior to the event. At the
time of the event, there were no maintenance manual requirements
for an EEC stored faults check following an engine run after
replacement of the FMU. Maintenance personnel noted, then cleared,
the fault codes from the computer memory and the engine was
successfully test run. They then chose to remove both the right
engine FMU and the EEC for further testing. The EEC unit was sent
to the engine manufacturer for bench testing and operating on a
test bed engine.
Component testing
The FMU manufacturer's testing found no faults in the unit.
Initial testing of the EEC by the engine manufacturer could not
duplicate, on the test bed engine, the dual channel failure and
subsequent shutdown. Analysis of the fault codes recorded by the
operator's technicians following the event confirmed that several
FMU electrical related fault codes were pre-existing on Channel A
of the EEC at the time of the occurrence. When the engine
manufacturer repeated the testing with the recorded fault codes
entered into Channel A of the EEC, and simulated loss of Channel B,
they successfully repeated the dual channel failure and resulting
engine shutdown.
Electronic engine controller
The electronic engine controller was a two-channel (Channels A
and B) electronic unit with system redundancy. It controlled, among
other items, engine start sequencing, power requirements, operating
temperature, turbine speeds, fuel flow, engine monitoring, and
automatic relight. It contained fault detection, storage, and
readout capabilities, all stored on an electrically
erasable/programmable read-only memory (EEPROM) located on a
computer board assembly. The EEPROM provided a history for
troubleshooting purposes of any fault event within the EEC or
associated control systems by logging a fault code of the event.
Those fault codes were then stored until intentionally cleared
during maintenance action. The distinct two-channels in the unit
ensured that should one channel fail, the other would assume
control and monitoring of the engine. Testing by the engine
manufacturer revealed that repeated random access memory (RAM)
parity errors in Channel B of the EEC resulted in repeated multiple
resets of the channel. Those repeated resets had proven to result
in a loss of Channel B functionality.
Engine rotation during restart attempts
Following the event, the flight crew stated that they could not
obtain a windmilling engine N2 (gas generator RPM) value of 14% as
required in the emergency procedures for restart of the engine.
They stated that the maximum engine N2 witnessed was 8%.
The engine manufacturer recommended a 14% N2 value
(approximately 2,380-RPM) at fuel introduction during engine
starting procedures. That allowed a cooler start and prevented
engine deterioration. The value of 8% N2 for the ALL ENGINE
FLAMEOUT emergency windmilling procedure was based on the minimum
engine-driven fuel pump pressure to open the engine pressurising
valve. The airframe manufacturer reported that windmilling flight
tests were successfully demonstrated at airspeeds as low as 240
knots with N2 windmilling rotor speeds as low as 8%.
The airframe manufacturer estimated that at a stable condition
of 10,000 ft altitude, and 250 knots indicated airspeed, the
occurrence engine should have exceeded 10% N2 before engine start
switch engagement. Their review of the digital flight data recorder
(DFDR) revealed no evidence of N2 increase as would be seen with
engine starter engagement. The airframe manufacturer reported that
their understanding was that the anomalies experienced during the
event would have prevented the starter air valve opening during the
restart attempts.
Flight data recorder
Examination of the recording indicated that the aircraft arrived
at the destination and then departed on another flight to the
north. The reported ground runs had not been recorded, as required
by Civil Aviation Order (CAO) 20.18 Section 6 paragraph 6.6.
Australian CAO 20.18 Section 6 paragraph 6.6 stated, "The
operator of an aircraft which is required by this section to be
equipped with recorders shall take action to ensure that during
ground maintenance periods the recorders are not activated unless
the maintenance is associated with the flight data recording
equipment or with the aircraft engines."
Australian CAO 20.18 Section 6 paragraph 6.3 stated, "Where an
aircraft is required to be so equipped by this section, the flight
data recorder system shall be operated continuously from the moment
when the aircraft commences to taxi under its own power for the
purpose of flight until the conclusion of taxiing after
landing."
The intent of the Australian legislation was that when an
aircraft commenced taxiing under its own power for the purpose of
flight, the flight data recorder (FDR) would record until the
aircraft was parked at the conclusion of the flight. That action
ensured a continuous record of aircraft operation was maintained
for the duration of the flight.
Subsequent Enquiries made to Boeing Long Beach Division, the
aircraft manufacturer, revealed that when the aircraft park brake
was set, the FDR would cease recording. Boeing Long Beach Division
stated that the FDR would begin recording by two methods. The first
"normal" recording mode activated when either fuel shutoff switch
was set to run and the park brake was released. The second
"maintenance" recording mode was activated by accessing a FDR RUN
command via the Multifunction Control Display Unit.
Aircraft Australian certification
The Boeing 717-200 was issued a Type Acceptance Certificate in
accordance with Civil Aviation Regulation, (CAR) 21.29A which
allowed Type Certificate acceptance for imported aircraft certified
by the National Airworthiness Authority (NAA) of a recognised
country, in this case the United States of America. The Boeing
717-200 aircraft may not comply with the appropriate Australian
Civil Aviation Regulations and associated Orders.