The Sikorsky S76C helicopter was in cruise flight with the automatic flight control system engaged, when the flight crew noted a loud noise and the helicopter yawed to the left, rolled left, and the nose pitched down. The flight crew disengaged the automatic flight control system and resumed flying the helicopter manually, stabilising it in level flight. The right engine-out and fire-warning annunciators were illuminated, with the engine-out aural warning sounding. The right engine instruments displayed zero rotational speed of the gas generator (GG) and extremely high turbine outlet temperature (measured at point T4 within the engine). The crew activated the right engine fire bottles and simultaneously closed the fuel firewall shut-off valve. The fire indication extinguished. They then configured the helicopter for single engine flight with the remaining engine operating approximately ten seconds into the two and one-half minute One Engine Inoperative (OEI) limitation. The flight crew adjusted power requirements for the OEI condition and then completed an uneventful single engine landing at their Longford base.
Examination of the helicopter revealed minor shrapnel damage to the right engine exhaust extension, and fracture separation of the engine oil pressure switches and rear bearing external oil vent and return pipes.
The Turbomeca Arriel model 1S1 engine comprised five modules. Module three (or the high-pressure section) contained the gas generator first and second stage wheels. The left side of the right engine, forward of the external rear bearing oil return line near the outer surface of module three, displayed evidence of fire and oil residue.
The right engine was removed and shipped to the engine manufacturer's Australian facility for disassembly and examination with Australian Transport Safety Bureau (ATSB), operator, and engine manufacturer representatives in attendance.
Engine examination
Disassembly and preliminary examination of Arriel 1S1 engine, serial number 15038, revealed a separation of one GG second stage turbine blade. Blade number sixteen was separated above the blade 'fir tree' attachment point, below the blade platform, and had punctured the second stage nozzle guide vane turbine ring. The rear bearing of the GG had collapsed and was significantly damaged. Separated pieces of the centrifugal diffuser of module three were found inside the module. There were indications that several fracture surfaces of the separated sections were pre-existing before the incident. In addition, the engine exhibited signs of severe overheating and significant damage in the air path downstream of the turbine blade separation.
The fracture surface of the separated blade was typical of ductile tensile overload, with the exception of the small corner area of fatigue cracking. The dendritic patterns within the fracture were indicative of the normal underlying microstructure of the blade casting. Failure of the blade in that mostly ductile overload manner indicated exposure to a transient or sustained stress level above the ultimate strength of the blade material at its operating temperature. Refer to ATSB Technical Analysis Report 200103038 (BE/200100017) for further details.
Engine history
The engine was installed on 4 March 2000 and had accumulated 7,935.0 hours and 6,784.1 cycles since new. It had been overhauled on 12 February 1999, and had accumulated 1,992.0 hours time since overhaul (TSO) and 1,878.1 cycles since overhaul. The GG assembly second stage turbine disc, serial number DC3666YC, had been installed during the overhaul with zero hours and cycles accumulated. The turbine disc and blades were well within the life limit of 10,000 cycles established by the manufacturer. Arriel engine modification TU204 (GG turbine blade plasma coating) had been incorporated.
Previous Australian occurrences
Occurrence report 200100584
On 7 February 2001, a Sikorsky S76C helicopter belonging to the same operator, with two crew and ten passengers on-board, was in a hover with the flight crew completing before take-off checklist items. The pilot reported that while trimming the engines, a "pop" was heard. He then noted that the left engine turbine gas temperature (measured at point T4 within the engine) was in excess of 1000 degrees C. The helicopter was then landed uneventfully. The flight crew reported that the only cockpit indication of imminent failure was the almost simultaneous illumination of the left engine chip (magnetic particle) detector advisory.
Examination of the helicopter revealed minor shrapnel damage to the left engine exhaust extension and engine cowling. There was no reported engine fire. The left engine was removed and sent to the engine manufacturer for disassembly and examination. The manufacturer's final report noted a separation of turbine blade number six of the GG second stage disc. The blade was separated above the 'fir tree' attachment point but below the blade platform, and had punctured the second stage nozzle guide vane turbine ring. One adjacent blade (number seven) in the direction of turbine wheel rotation was also noted as cracked.
Metallurgical examination by the manufacturer attributed the blade failure to a low-cycle fatigue cracking mechanism. The manufacturer concluded that abnormal loading was the major contributing factor in the failure, given the reported absence of anomalous material features or evidence of high-temperature operation. Dimensional inspections failed to reveal any sign of non-conformity that could have led to the development of the abnormal loads. However, the manufacturer stated that turbine blade platform/GG disc interferences were also a potential factor that could have aggravated the fatigue failure of the blade.
At the time of the occurrence, Arriel 1S1 engine, serial number 15522, had accumulated 4,737.4 hours and 4,471 cycles since new. It had accumulated 1,740.0 hours TSO and 1,615 cycles since overhaul. Following overhaul, the engine was installed on March 11, 1999. Module three did not have turbine blade plasma coating modification TU204 incorporated.
Occurrence report 199602839
On 9 September 1996, a Sikorsky S76C helicopter belonging to the same operator, experienced an in-flight engine failure of the right engine while taking off from an oil platform. A loud noise was heard before the engine failure. The right engine was shut down and the crew completed an uneventful single engine return to the Longford base. There was no reportedassociated engine fire. The right engine was removed and sent to the manufacturer fordisassembly examination.
At the time of the occurrence, Arriel 1S1 engine serial number 15513, had accumulated 2,282.0 hours and 1,949 cycles since new. The manufacturer provided the operator with a final report noting the rupture (separation) of one GG turbine blade with subsequent rear bearing damage and GG seizure. Their report stated that the separation was suspected to be the result of blade rubbing with the second stage nozzle guide vanes with no signs of fatigue or abnormal over temperature operation. Module three had turbine blade plasma coating modification TU204 incorporated.
Other overseas occurrences
The French airworthiness authority, Direction Generale de l'Aviation Civile (DGAC), reported knowledge of three other overseas occurrences involving GG second stage turbine blade separation failures. Of those three incident engines, all had the TU204 modification. Cycles since overhaul on those incident engine turbine discs and blades varied from 1,978 to 5,933 cycles.
Engine service bulletin history
Turbomeca Service Bulletin (SB) 292 72 0151 was originally issued on 5 June 1992 specifying the incorporation of modification TU204, the protection of the GG second stage turbine blades from corrosion or erosion with a Heurchrome low pressure plasma coating. That modification also permitted a performance improvement by allowing the more accurate machining of the turbine tip diameter to control the tip clearance. The service bulletin addressed all Arriel variants, with Arriel 1S1 engines having incorporated TU204 from the first production engine. For all other variants, TU204 implementation was optional and installed at the customers' request.
In July 1998, the engine manufacturer implemented internal documentation and procedures to remove all GG turbine blades with TU204 installed during overhaul of module three. Consequently, SB 292 72 0151 was amended on 18 August 2000, to recommend removal of all TU204 modified blades, citing possible weight mass increases and suspected increased stress on the turbine blade root. The manufacturer stated that if the plasma coating was not applied as per drawing requirements, the resulting stresses could be more than anticipated, resulting in abnormal loading of the blade root. Both incorporation and removal of modification TU204 required removal of the engine and/or module and shipment to the manufacturer.
External oil pipe description
Three external oil related pipes provided lubrication of the GG rear bearing. Those pipes passed through hollow support struts and were then physically secured to module three. The supply oil pipe provided oil from the engine driven gear type oil pump to the bearing after passing through a restrictor and a tube screwed into the bearing housing. Oil was then sprayed onto the bearing. After lubricating the bearing, the oil fell by gravity to the bottom of the housing, through a tube and was returned to the tank through an oil pipe to the scavenge pump. The air/oil mist that resulted from the lubrication of the bearing was vented overboard through a vent pipe attached to the top of the housing.
Engine oil flashpoint/autoignition
The engine oil temperature of a normally operating Arriel 1S1 engine in a S76C helicopter was approximately 100 degrees Celsius (C). The flash point of the turbine engine oil was approximately 223 degrees C. The flash point of a liquid was defined as the lowest temperature at which a material would produce a flammable vapour, and was a measure of the volatility of the material.
The auto-ignition temperature of engine oil was approximately 388 degrees C. Auto-ignition temperature was defined as the temperature at which auto-igniting materials spontaneously combust. According to the engine manufacturer, during normal operation, the external surface temperatures of number three modules ranged between 280 to 450 degrees C, dependent upon location on the module, with a maximum surface temperature of 450 degrees nearest the rear bearing. The surface temperature maximum values of module three were well within the auto-ignition temperature of the engine oil.