Investigation number
200101782
Occurrence date
Location
83 km W Dalby (ALA)
State
Queensland
Report release date
Report status
Final
Investigation type
Occurrence Investigation
Investigation status
Completed
Highest injury level
None

While cruising at FL140, the pilot in command of the Brasilia noticed a torque drop from 84% to 74% on the right engine. Assuming that the power lever friction was loose and had allowed the engine to creep back from the selected power setting, he readjusted the lever position back to 84% and reset the friction. Approximately 10 seconds later the non-flying pilot remarked that the right engine torque had dropped to 76%. As the pilot in command again went to readjust the torque, the engine lost power. The aircraft then yawed significantly.

The crew then shut down the engine and feathered the propeller. As the aircraft was flying into a 40 to 50 knot headwind, the crew decided to return to the departure airfield.

Company maintenance investigation found that the hydro-mechanical unit (HMU) on the right engine had malfunctioned. The HMU was removed and forwarded to the vendor for further investigation. A serviceable HMU was fitted to the right engine and the aircraft returned to service.

Aircraft Details
Manufacturer
Embraer-Empresa Brasileira De Aeronautica
Model
EMB-120
Registration
VH-XFX
Serial number
120-116
Operation type
Air Transport Low Capacity
Sector
Turboprop
Departure point
Brisbane, QLD
Departure time
1723 EST
Destination
Roma, QLD
Damage
Nil