Investigation number
199901064
Occurrence date
Location
54 km NNW Launceston, (VOR)
State
Tasmania
Report release date
Report status
Final
Investigation type
Occurrence Investigation
Investigation status
Completed
Occurrence class
Incident
Highest injury level
None

The right engine of a Fairchild Metro II aircraft, VH-EEQ, failed at the top of descent to Launceston. The aircraft subsequently completed an uneventful single-engine landing. On-site inspection revealed that the engine failure was caused by the disintegration of the second-stage turbine wheel and that segments of the wheel had penetrated the engine nacelle. One fragment penetrated the fuselage and was found lodged in the cabin lining.

The AlliedSignal TPE331-3U-304G engine, serial number P03214C, was reported to have completed 6,017.4 hours and 6,273 cycles since new.

The second-stage wheel was identified as part number 868272-1, serial number 1-01345-1313. The recorded history of the second stage wheel indicated that the wheel had been in service for a total of 2,972.84 hours and 2,878 cycles at the time of failure on 5 March 1999. The wheel was installed new in engine s/n P90105 on 11 Jan. 1982. It was removed from engine s/n P90105 on 25 Sept. 1992 with a recorded service life of 564.74 hours and 508 cycles. The wheel was installed in engine s/n P03214C on 30 Aug. 1994 with a recorded history of 564.74 hours and 508 cycles in service. There remain, however, uncertainties in the recorded service history of the part.

Aircraft Details
Manufacturer
Fairchild Industries Inc
Model
SA226
Registration
VH-EEQ
Serial number
TC-251
Operation type
Charter
Sector
Turboprop
Departure point
Melbourne, VIC
Departure time
0305 hours ESuT
Destination
Launceston, TAS
Damage
Minor