The flight, using a Cessna 210 aircraft, had been arranged as a
charter after the scheduled regular public transport (RPT) service
aircraft had become unserviceable. Waiting passengers were advised
of the cancellation of the scheduled service and that limited
seating would be available on a charter flight. Five passengers
elected to take the charter flight using their previously purchased
tickets and the company agent briefed them on the changed status of
the flight.
Subsequently, while cruising at an altitude of 4,500 ft, the
pilot reported to Adelaide flight service that the engine was
running rough, that the engine cylinder head temperature (CHT)
indication had become very high and that she was attempting to
locate a clear area for a forced landing. The pilot landed the
aircraft in a cleared gravel pit. During the landing roll however,
the aircraft struck large mounds of gravel and was substantially
damaged. The pilot and several passengers sustained serious
injuries.
The aircraft came to rest upright, resting on the lower fuselage
and right wingtip, with the tricycle landing gear folded back under
the aircraft. The left wing was damaged with fuel escaping from the
wing fuel tank. The engine had separated from the airframe and came
to rest inverted in front of the wreckage.
The passengers evacuated the aircraft and assisted the
unconscious pilot from the cabin. Adelaide flight service arranged
for overflying aircraft to locate the accident aircraft and
coordinated a rescue team to be dispatched from Darwin. A
search-and-rescue (SAR) helicopter attended the scene and took the
occupants to Darwin for medical attention.
The aircraft carried a manually operated GME Electrophone MT310
portable emergency locator transmitter (ELT), however the
passengers were not aware of its location. Although the injured
pilot attempted to direct the passengers to the ELT in the
aircraft, the passengers were unable to locate it and as a result
the ELT was not activated.
Aircraft engine
The aircraft was fitted with a Teledyne-Continental IO-520-L
engine, serial number 567962, that had completed 734.5 hours since
being overhauled. The engine was removed to a suitable engine
maintenance facility for examination which revealed that the number
one cylinder head had cracked, resulting in the observed high
cylinder head temperature and rough running reported by the pilot.
The cylinder head, part number TM642320F, had 10/81 stamped on the
rocker boss, indicating that the cylinder head had been
manufactured in October 1981. The history of the cylinder head,
including the total time in service, could not be determined.
A detailed metallurgical examination of the cracked cylinder
head determined that the cylinder head had failed as a result of
fatigue cracking due to overheating (See Technical Analysis
Report).
The engine was fitted with a six-point cylinder head temperature
sensing system with a temperature sensor probe in the head of each
cylinder. However, this system was inoperative at the time of the
occurrence. A single, ring-type temperature sensor was fitted to
the number one cylinder lower spark plug, in addition to a standard
spark plug washer. Normally, a ring-type temperature sensor
replaces the spark plug washer. This sensor provided cylinder head
temperature information to the aircraft cylinder head temperature
gauge. A maintenance release entry, dated 27 September 1998, stated
"CHT guage drops to zero periodically".
The engine baffles, used to direct cooling airflow over the
engine cylinders, were in a generally poor condition with several
cracks, broken mounting rings and worn areas. In one place, a
baffle had been worn through by contact with an engine hose.
The engine had been overhauled on 18 August 1997 and fitted with
six overhauled cylinders. On 11 August 1998, the number four
cylinder head had failed because of cracking and was replaced. On
28 August 1998, the number six cylinder head had similarly failed
because of cracking and was replaced. On 14 October 1998, 16.4
flying hours before the accident, the engine had passed a cylinder
pressure leak check during routine maintenance.
Piston engine maintenance requirements
The Australian Civil Aviation Safety Authority (CASA)
airworthiness directive, AD/ENG/4 (Amdt 7), details continuing
airworthiness requirements for piston engines. That directive
requires piston engines, operated in charter operations, to be
overhauled in accordance with the engine manufacturer's
requirements or in accordance with an approved system of
maintenance. The directive also requires that the engine service
history be recorded in the engine logbook. The engine manufacturer,
Teledyne Continental Motors (TCM), does not specify retirement
lives for engine cylinders but advises that "at some point in
operating hours, generally very high, the aluminium cylinder head
will fatigue due to the cylinder pressure loads and temperatures."
TCM also advise that for cylinders in excess of two overhaul cycles
"past that, duty cycle and the nature of field repairs make it
difficult to project future life."
TCM also report that cylinder head life can be affected by any
detonation/preignition event during the cylinder life, and that hot
cylinder operation due to poor baffles or fuel mismanagement has a
significant effect. CASA's information brochure titled "Piston
Engine Cylinders" also recognises that those components have a
limited life and suggests that cylinders be replaced every second
or third engine overhaul. However, piston engine cylinders are not
required to have serial numbers and recorded life history in the
same manner as their parent engine.
Data review
A review of ATSB data covering the 10-year period January 1990
to December 1999 revealed that there had been over 60 reported
occurrences, including a number of forced landings, involving
piston engine cylinder head structural failures. Only one other
reported cylinder head failure during this period resulted in
occupant injuries. A review of the CASA major defect reporting
(MDR) system for the same period revealed that there had been about
250 reported piston engine cylinder head structural failures, an
average of approximately one failure every 2 weeks. The data only
records the proportion of cylinder failures that have been reported
through formal reporting procedures. Other cylinder head failures,
such as those detected during routine maintenance, are possibly not
represented.