What happened
On 21 January 2017, at about 0710 Eastern Standard Time (EST), the pilot of an Air Tractor AT‑401B aircraft, registered VH-DDW, was conducting aerial spraying operations at a property about 10 km NW of Mareeba Airport, Queensland. The pilot was the only person on board the aircraft.
Part way through spraying the load of chemical on an avocado plantation, the pilot climbed the aircraft at the end of a spray run, to about 200 ft above ground level. As the aircraft climbed, the engine suddenly made loud banging noises and the pilot estimated that the engine power reduced by about half.
Figure 1: Location of engine failure and accident site
Source: Google earth annotated by ATSB
The pilot levelled the aircraft and checked the fuel mixture and throttle controls but the engine did not respond. The power available continued to decrease as the pilot looked ahead for a suitable field to conduct a forced landing. The pilot selected a cleared area, but as the aircraft lost height, they realised that the aircraft was not going to make it to that field.
The pilot then radioed their loader driver[1] and advised that they had engine trouble, the aircraft was ‘going down’, and asked them to contact emergency services. The loader driver had heard the abnormal noise the aircraft’s engine was making, and responded immediately to the pilot.
As the aircraft descended, the pilot sighted powerlines ahead and assessed that the aircraft would probably not make it over them. Therefore, the pilot descended to pass under the powerlines. The pilot again spoke to the loader driver briefly on the radio. The aircraft then collided with several lychee trees and a vehicle that was parked in an orchard. The aircraft came to rest upright and was substantially damaged. The pilot sustained a minor injury.
Figure 2: Damage to VH-DDW
Source: Pilot
Operator report
The operator conducted an investigation into the accident and found the following:
The pilot had conducted a daily inspection, including an inspection of all engine cylinders, and found no signs of cracks. The aircraft had operated normally during the first two flights that day.
The aircraft was fitted with a Pratt and Whitney R-1340 radial engine that had 10,491 total hours and 478.1 hours since overhaul. The engine was inspected after the accident by a representative from an aircraft maintenance organisation and they determined that the number seven cylinder had failed (Figure 3). A crack was located around the circumference of the cylinder head, between the two spark plug holes. A recurring inspection of this area (CASA airworthiness directive AD/PW-P/19) was conducted about 91.9 hours prior to the accident at the periodic (100 hourly or 12-month) maintenance inspections.
Figure 3: Engine cracked number seven cylinder
Source: Aircraft operator, modified by the ATSB
Safety analysis
Post-accident inspection
A post-accident inspection revealed a cracked cylinder.
Pre-flight inspection
The aircraft had operated for about 91.9 hours since the periodic (100 hourly or 12-month) maintenance inspections.
The pilot conducted a pre-flight inspection at about 0500 and everything was normal, the oil was full. The aircraft was fitted with a chip detector,[2] which did not activate at any time. The engine indications indicated normal temperature and pressure immediately prior to the failure.
Weather and performance
The aircraft took off from Mareeba Airport, which is at an elevation of about 1,560 ft above mean sea level (AMSL), and was operating over a property at about 1,900 ft AMSL. The temperature was about 24 °C and there was 79% humidity. The conditions on the day may have reduced the aircraft’s performance. The pilot had substantial experience operating that aircraft in the local area.
The wind was a light westerly at about 2 kt and when the engine lost power the aircraft was tracking to the east, therefore with a light tailwind. This probably did not significantly affect the glide distance or the landing speed of the aircraft.
Forced landing sites
The area has orchards, houses and powerlines in most of the paddocks with uneven ground and creeks running through it, therefore there were limited sites suitable to conduct a forced landing. The pilot assessed that there was also no suitable road within gliding distance. The accident site was about 2.5 km from where the engine failed.
Chemical load
About 750 L of chemical was still on board the aircraft when the engine lost power. The pilot did not dump the load. The pilot commented that it was an oversight rather than a conscious decision not to dump the load. However, they further commented that they were trained to dump the load in the event of engine failure, and would do that in future if faced with a similar situation.
Findings
These findings should not be read as apportioning blame or liability to any particular organisation or individual.
- The number seven cylinder cracked, resulting in a loss of power.
- The aircraft was operating at low level (below 200 ft AGL) in an area where there were limited options available to conduct a forced landing.
Safety message
In this accident, the time available to manage the engine failure meant that there were few options in regards to the selection of a landing area. The accident highlights the importance of taking positive action and maintaining aircraft control when conducting a forced landing, while being aware of flare energy and aircraft stall speeds.
The Aerial Agricultural Association of Australia advised that there is nearly always an uncertainty about whether to dump the load and they suggest that the only safe rule is ‘if in doubt, dump’. In a high stress situation such as an engine failure where there is limited time, it is important to apply appropriate emergency procedures. To mitigate against the effect of stress compromising memory even in a minor emergency, pilots should have embedded motor programs to handle emergencies in reactive mode.
The pilot was wearing a helmet and commented that although they were ‘flung’ from side to side during the accident sequence, the seatbelt held them firmly in place.
Aviation Short Investigations Bulletin - Issue 59
Purpose of safety investigationsThe objective of a safety investigation is to enhance transport safety. This is done through:
It is not a function of the ATSB to apportion blame or provide a means for determining liability. At the same time, an investigation report must include factual material of sufficient weight to support the analysis and findings. At all times the ATSB endeavours to balance the use of material that could imply adverse comment with the need to properly explain what happened, and why, in a fair and unbiased manner. The ATSB does not investigate for the purpose of taking administrative, regulatory or criminal action. TerminologyAn explanation of terminology used in ATSB investigation reports is available here. This includes terms such as occurrence, contributing factor, other factor that increased risk, and safety issue. Publishing informationReleased in accordance with section 25 of the Transport Safety Investigation Act 2003 Published by: Australian Transport Safety Bureau © Commonwealth of Australia 2017 Ownership of intellectual property rights in this publication Unless otherwise noted, copyright (and any other intellectual property rights, if any) in this report publication is owned by the Commonwealth of Australia. Creative Commons licence With the exception of the Coat of Arms, ATSB logo, and photos and graphics in which a third party holds copyright, this publication is licensed under a Creative Commons Attribution 3.0 Australia licence. Creative Commons Attribution 3.0 Australia Licence is a standard form licence agreement that allows you to copy, distribute, transmit and adapt this publication provided that you attribute the work. The ATSB’s preference is that you attribute this publication (and any material sourced from it) using the following wording: Source: Australian Transport Safety Bureau Copyright in material obtained from other agencies, private individuals or organisations, belongs to those agencies, individuals or organisations. Where you wish to use their material, you will need to contact them directly. |
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- Ground personnel responsible for loading the chemical into the aircraft for spraying.
- A magnetic device used to gather chips of metal from engine or transmission oil to provide early warning to maintenance personnel of impending engine failure. Depending on the installation, it can be linked to an in-cockpit indicating light to provide immediate advice to aircrew.